Hearing loss was the second-most common illness reported to the Mine Safety and Health Administration (MSHA) in 2009. Furthermore, between 2000 and 2010, 30% of all noise-related injury complaints reported to MSHA were for coal preparation plant employees. Previous National Institute for Occupational Safety and Health (NIOSH) studies have shown that vibrating screens are key noise sources to address in order to reduce coal preparation plant noise. In response, NIOSH researchers have developed a suite of noise controls for vibrating screens consisting of constrained layer damping (CLD) treatments, a tuned mechanism suspension, an acoustic enclosure, and spring inserts. Laboratory testing demonstrates that this noise control suite reduces the A-weighted sound power level of the vibrating screen by 6 dB. To provide a comparison to laboratory results and prove durability, field testing of two noise controls was performed on a vibrating screen in a working coal preparation plant. The spring inserts and CLD treatments were selected due to their ease of installation and practicability. Field testing of these controls yielded reductions that were comparable to laboratory results.
Of all occupational illnesses reported to the U.S. Bureau of Labor Statistics in 2004 and 2005, 11% were due to noise-induced hearing loss (NIHL)
The Office of Mine Safety and Health Research (OMSHR) Hearing Loss Prevention Branch (HLPB) develops such noise controls for miners. One area where the OMSHR HLPB has focused its research is within coal preparation plants. According to MSHA data, 30% of all noise-related injury complaints since the year 2000 have involved preparation plant employees. In 2009, there were 37,405 employees at mine facilities with preparation plants and 8,343 workers who were categorized as preparation plant employees at these facilities
A recent NIOSH study shows that 43.5% of employees within preparation plants are overexposed to noise. Furthermore, the study found that not only were vibrating screens one of the loudest pieces of equipment at the preparation plants, they were also the most numerous, thus making vibrating screens a key noise source to address
A horizontal vibrating screen (
The screen is designed in such a way that it vibrates on roughly a 45-degree angle from horizontal. In operation, coal flows into the feed end of the screen from a delivery chute. As the screen vibrates, the material moves along the deck and under a water spray that rinses the coal. The liquid and fine coal particles pass through the gaps in the screening deck as the material flows toward the discharge end of the screen. Finally, the rinsed coal falls off of the discharge end of the screen to continue with further processing.
In general, there are two primary mechanisms of noise generation on a vibrating screen: material flow noise generated from either impacts between the material and the screen surfaces or between individual pieces of the material itself, and noise generated by vibration of the screen through its operation. As Ungar et al. notes, “In general, coal impact noise predominates in screens handling coarse coal, and drive mechanism noise predominates in screens handling finer coal
Previous NIOSH studies of a horizontal vibrating screen used to process clean coal at a preparation plant indicated that noise due to vibration of the screen itself was the dominant noise source, whereas noise from material flow was less significant
As a consequence, a unique noise control solution was necessary for the screens under study in this project. Prior noise source identification studies in the lab showed that screen body noise is the main noise source below about 1 kHz, while mechanism housing noise is the primary source above 1 kHz. The sound energy at frequencies below 1 kHz accounts for about 80% of the overall A-weighted sound power level. In addition, operating deflection shape analysis revealed significant response on the screen sides and feedbox
Other researchers have attempted some novel solutions for controlling screen noise for the sources listed above. Several researchers have recommended treatment of the screen body panels and cross beams with free-layer or constrained-layer damping
To address the excitation noise of the screen, which includes the motor, eccentric mechanisms, and drive belt, several different designs have been developed. Jakobs
Enclosures have also been commonly recommended to reduce screen excitation noise. Most of the enclosures employed have been for the entire screen
As mentioned above, the common solution to reducing spring noise is to use rubber isolators. Alternate solutions have been to redesign the spring supports to use multiple lower-stiffness springs
This work is unique in that the noise controls’ effectiveness has been determined by measuring sound power in the lab per ISO 3743-2
All measurements were taken on a Conn-Weld 2.44-m × 4.88-m (8-ft × 16-ft) horizontal vibrating screen with dual G-Master 1000 vibration mechanisms, as shown in
Temperature measurements were made for those noise controls installed on the vibrating screen that had an effect on mechanism temperatures. To avoid mechanical failure of the bearings or other components, the screen manufacturer, Conn-Weld, recommends that the mechanisms run at a maximum temperature of 82.2°C (180°F) for standard oil and an absolute maximum temperature of 90.6°C (195°F) for high-temperature oil when measured at the surface of the housings. A variety of cooling methods were attempted to keep the operating temperature within acceptable limits after the noise controls were installed.
Five type J thermocouples were connected to the mechanism housings with thermally conductive cement (
Baseline measurements of the vibrating screen reveal a bimodal distribution of sound energy with an overall A-weighted sound power level of 100.5 dB, as shown in
A suite of noise controls was designed to address the different noise sources discovered on the vibrating screen. The spring inserts were designed to eliminate spring chatter as a noise source and to ensure testing repeatability because the level of spring chatter was highly variable. The constrained layer damping treatments and acoustic enclosure were applied to the mechanism housings to reduce their contribution to the frequencies above 1 kHz. The tuned mechanism suspension was designed to reduce screen body noise below 1 kHz by decoupling the mechanical energy of the mechanisms from the noise-radiating structure of the screen body.
Spring inserts were designed to eliminate spring chatter noise by preventing the last full coils and the cut and ground coils on each of the spring ends from coming into contact. An earlier prototype of the inserts, tested in the lab, was a curved slab of 70 durometer natural rubber with tapered grooves to seat the spring coils. The final inserts developed for field testing were composed of 70 durometer natural rubber bonded to a 6.4-mm-thick (1/4-inch-thick) curved steel shell along the outer perimeter. The steel shell was intended to provide a striking surface for hammering the spring inserts into place between the spring coils. The rubber portions of the inserts were tapered to match the contours of the springs for better contact, and had a lip to prevent them from sliding out of place during screen operation, as shown in
Constrained layer damping (CLD) is commonly used to treat a vibrating surface that is generating noise. It consists of a layer of flexible damping material applied to the vibrating surface, with the other side of the damping layer constrained by a more rigid material such as steel. Vibration energy from the base layer is transformed into a shear deformation within the damping layer, which reduces the noise radiated by the system while generating a small amount of heat.
For this application, a thin sheet of 80 durometer, 0.64-mm-thick (0.025-inch-thick) elastomeric damping material was bonded on one side to the flat faces on the front, top, and back of each mechanism housing using epoxy. These layers of damping material were then constrained by being bonded to 6.4-mm-thick (1/4-inch-thick) steel plates.
A tuned mechanism suspension (TUMS) was developed to selectively transmit forces at the mechanism rotation speed of 900 RPM, while attenuating forces at higher frequencies that resulted from the gears and bearings. The mechanism suspension is “tuned” by adjusting the spring rates of the mechanism suspension to shift the rigid body resonant frequencies of the screen with the added mechanism suspension to either a higher or a lower frequency. In a previous publication
The TUMS consisted of a mounting plate, or “raft,” for the mechanisms, a modified H-beam, a series of gussets to support the added material to the H-beam, and a series of two-piece vibration isolators between the raft and the H-beam, as shown in
The H-beam was modified by adding a “cap,” as illustrated in
An acoustic enclosure was designed that surrounds both mechanism housings and is attached to the H-beam
As shown in
Enclosure construction involved a variety of materials and screen modifications. The frame was composed of steel angle stock and U-channel. It was isolated from the H-beam using strips of 57 durometer natural rubber. Panels were fabricated with 3.2-mm-thick (1/8-inch-thick) Dynalam™ damped steel (a CLD steel). The insides of the panels were lined with 25.4-mm-thick (1-inch-thick) Polydamp® acoustic foam. A boss made of 57 durometer natural rubber isolated the right panel from the bearing cover plate.
Because the enclosure consists of damped steel panels and is lined with acoustic foam, it makes a good thermal insulator. As a consequence, temperatures at the mechanism housings increase with the enclosure installed. A variety of methods to cool the enclosure were explored, including cooling the entire enclosure with compressed air, adding an 80.2-L/s (170-CFM) push–pull fan system at the inlet and exhaust ducts of the enclosure, exhausting the enclosure air with a 330.3-L/s (700-CFM) fan attached to a modified enclosure duct, and running this same fan at 75% airflow.
Early in the project, we observed spring chatter both in the lab and in the field. Later, through a beamforming study, it was shown that the suspension springs were one of the three main noise sources of the screen
After eliminating the spring chatter with the spring inserts, the next controls installed were the constrained layer damping treatments. As shown in
The TUMS system was installed on the screen next, in addition to the spring inserts and CLD plates. With the original 67 durometer vibration isolators, the bolt heads impacted against the modified H-beam, causing the noise to increase during operation. The sound power level increase was primarily due to a lack of clearance between the mechanism bolt heads and the modified H-beam.
In addition, the first set of vibration isolators was not stiff enough to hold all of the components together during operation. Examining the operation of the screen with a stroboscope revealed that the tops of the isolators were losing contact with the top of the modified H-beam. When the two-piece mounts are installed, the mounts are pre-compressed so that both the top and bottom of the mounts undergo static deflection. Because the top half of the isolator is slightly stiffer than the bottom half of the isolator, the static deflection of the top half of the isolator is slightly less than the static deflection of the bottom half of the isolator. The relative motion between the raft and the modified H-beam exceeded the static deflection of the top half of the isolator. This caused the top half of the isolator to become unloaded and allowed separation of the isolator from the top of the H-beam.
Several changes were made to address these problems. The height of the isolator tops was increased to 3.2 cm (1.25 inch) to reduce the spring rate of the top half of the isolator relative to the bottom half. This ensured that the top half would have enough static deflection to prevent the components from separating under operation. The durometer of the mounts was also increased to increase the mount stiffness. Finally, various spacers were used to increase the preload on the vibration isolators and the clearance of the bolt heads from the modified H-beam, as shown in
Sound power level reductions were achieved with these design changes to increase preload, clearance, and mount stiffness.
Performance for individual 1/3-octave bands varied with durometer and preload, as shown in
Another concern in mount selection was heating of the mounts under operation, which caused the sound power level to increase over time. Previous measurements of failed mount configurations showed a trend of increasing sound power as the testing progressed. Thermocouples were installed on one of the earlier mount prototypes to observe how they were heating up. The results showed that the mount temperature increased as the vibrating screen continued to run. When the mount temperature reached 93.3°C (200°F), the test was aborted per the isolator manufacturer’s recommendation that the mount temperature should not exceed 93.3°C (200°F). Due to internal damping, the isolators heated up during operation as the rubber stretched and compressed. As the isolators increased in temperature, their stiffness was reduced. The design of the TUMS is such that the vibration mode characterized by relative motion between the raft and the modified H-beam occurs at a frequency much higher than the 15-Hz operating frequency of the screen. As the mount temperatures increase and the mount spring rates decrease, the frequency of this vibration mode shifts closer to the operating speed of the screen. This results in an increase in motion of the mechanisms, which in turn causes the impact forces within the gears and bearings to increase. The temperature increase is a probable cause for the increase in noise from the early prototypes.
While the 80 durometer mounts with spacers on top and bottom showed the greatest stability in terms of sound power levels over time, their overall poor performance in sound power level reductions eliminated them as a candidate. Removing the bottom spacers from the 80 durometer mounts caused the mounts to increase in temperature and exhibit the same trend of increasing sound power levels over time. However, the 90 durometer mounts showed a trend of decreasing sound power levels with time, suggesting that the ideal mount stiffness is between 80 and 90 durometer if the stiffness could remain constant with temperature. For durability concerns, the 90 durometer mount configuration with minimum preload was selected. This configuration yields a sound power level reduction from the CLD and spring insert combination of 1.4 dB (
Finally, an acoustic enclosure was added to the noise control package. Originally, the enclosure had been installed directly onto the H-beam in previous testing
As shown in
As a consequence of adding the acoustic enclosure, temperature data were taken as discussed previously to determine if the enclosure would cause premature damage to the bearings due to excessive heat. For all tests the thermocouple located at position 4 (see
Next, several cooling methods for the enclosure were evaluated. Because the free convection provided by the enclosure ducts was not sufficient for cooling, the enclosure was cooled using shop air, because that may be more convenient for the end user. An air line was run to the enclosure duct and an adapter was made for the duct-to-air line connection. However, the cooling performance was only slightly better than free convection, so this option was not pursued further. To create a push–pull system of airflow, 80.2-L/s (170-CFM) fans were then installed at the inlet and exhaust ducts. This showed moderate success (10 degrees cooler than the enclosure-only configuration after 4 hours), but because it was clear that the cooling was not sufficient, the test was aborted.
The final cooling configuration utilized a 330.3-L/s (700-CFM) exhaust fan. Additionally, the enclosure duct was modified to connect the top of the duct to a remotely located exhaust fan. As shown in
The 330.3-L/s (700-CFM) exhaust fan for the enclosure provides adequate cooling. However, further efficiencies could be gained by optimizing the cooling system to improve interior air flow. This may result in reduced airflow requirements for the fan. For example, the current duct configuration could be modified to reduce turbulence from bends and sharp corners. This has the potential to eliminate airflow losses in the duct. Further, during the testing described above for the 80.2-L/s (170-CFM) fans, the coolest mechanism housing temperature location at point 3 (
In order to prove the effectiveness of the noise control concepts that NIOSH had developed and the durability of the materials in the designs, NIOSH performed field testing at a nearby coal preparation plant in northern WV. If the noise controls in this testing were proven to be successful in a harsh production environment, then our industry partner would be able to incorporate these concepts into future designs. The preparation plant leadership expressed interest in trying two of the four laboratory-tested noise controls: the constrained layer damping (CLD) treatments and the spring inserts. These controls were selected for their ease of installation and practicability. The other noise controls require significant modification to the screen in order to be installed.
NIOSH researchers selected screen #169 (
However, it was not possible to study a machine in isolation at the preparation plant because of the control system in the plant. The plant is set up such that the bank of eight screens is split into two groups of four screens each, called Side 1 and Side 2. Side 1 or Side 2 may have the coal feed to their screens shut off, one screen in either Side 1 or Side 2 may be entirely shut down while the others continue to vibrate and process coal, and one side at a time may be entirely shut down. However, due to the required downtime involved and production needs, shutting down an entire side of the plant was not feasible. Thus, it was not possible to run only one screen with coal while shutting down all of the other screens.
Given the above constraint, in order to determine the effect of the noise controls, the influence from the surrounding machines had to be minimized. To accomplish this, the screen under test was isolated from its surroundings through the use of quilted acoustic barrier-absorber material to block and absorb a portion of the surrounding noise. To determine the effectiveness of the barrier-absorber material at reducing background noise, measurements needed to be taken before and after installation to determine the background noise reduction. Background noise was considered to be the noise due to all other machines in the plant except for screen #169. If background noise were reduced enough to minimize its effect on the overall levels, sound level measurements could then be made with the package of noise controls in place to determine their effect on the vibrating screen.
Six microphones were placed around the vibrating screen along the feed end and the left side to match previous testing conducted at the preparation plant
Three recordings of 30 seconds each were taken for each test configuration. The data were stored by a data acquisition system for post-processing. The same microphone locations and data acquisition system position were used for all measurements.
Quilted barrier-absorber material was installed around the perimeter of the screen as shown in
For each test, the average A-weighted 1/3-octave-band sound levels were calculated.
When the noise control package was installed, spring chatter noise had not been observed for the baseline. However, the spring inserts still needed to be evaluated for durability and ease of installation. Although the final prototypes of the spring inserts were originally designed to have an outer steel shell to aid in installation, the steel shell was found to be both problematic and unnecessary. First of all, prior to the field testing, it was determined that the prototype inserts for the inner spring did not fit within the outer spring, so all of the inner spring inserts were modified by removing the outer steel shell (
To determine the effect of the noise controls on overall sound levels, it is necessary to compare the data from all of the screens running with the barrier material in place versus the same conditions with the noise controls installed. This makes it possible to determine the reduction in sound level due to the noise controls. A comparison of these conditions in
A prior study conducted in the lab showed that the CLD plates alone reduced the overall sound power levels by 1 dB
NIOSH researchers at the Office of Mine Safety and Health Research developed four noise controls for a horizontal vibrating screen used in coal preparation plants. Spring inserts combined with constrained layer damping treatments on the mechanism housings reduced overall A-weighted sound power levels by 2.7 dB. The addition of a tuned mechanism suspension reduced the overall A-weighted sound power levels by an additional 1.4 dB. Finally, adding an enclosure to the noise control package improved the results by another 1.5 dB, which resulted in an overall reduction in A-weighted sound power level of nearly 6 dB—or a 75% reduction in A-weighted sound power—as a result of the entire noise control package. If implemented on all vibrating screens within a preparation plant, the entire noise control package has great potential to reduce overall levels in many areas of the facility.
To ensure that an acoustic enclosure would be practical to implement on a vibrating screen and that the mechanism temperatures would remain within the manufacturer’s limits, several cooling options were explored. A 330.3-L/s (700-CFM) exhaust fan for the enclosure running at 100% flow was found to provide sufficient cooling. A potential area for future work would be to design a more efficient cooling system by using lower-speed fans, redesigning the ductwork, and improving the air circulation within the enclosure. Better circulation of the air within the enclosure would be achieved by mounting fan blades on the spinning coupler ring between the two mechanism housings so that the air within the enclosure is mixed as the mechanisms turn. Better air mixing could potentially allow a shift-long run time with only the 80.2-L/s (170-CFM) fans. However, the current cooling system with the 330.3 L/s (700 CFM) fan does make it possible to utilize an acoustic enclosure in a production environment.
The two controls evaluated at the preparation plant—the CLD plates and spring inserts—met the dual goals of reducing sound levels and demonstrating sufficient durability in a production environment. However, for this particular trial, the spring chatter that the spring inserts are designed to address was not observed in the field prior to installation. When spring chatter was observed in the lab, the spring inserts and CLD plates in combination reduced the A-weighted sound power levels by 2.7 dB. The combination of spring inserts and CLD plates in the field reduced sound levels by 1 dB. Given the lack of pre-existing spring chatter in this case, it is unlikely that the spring inserts had any effect on the sound levels produced, and the reduction observed is likely due to the CLD plates alone. In this context, the field results are comparable to the laboratory results since prior lab testing showed a 1-dB reduction in the overall A-weighted sound power levels due to the CLD plates alone
Notably, this 1-dB reduction achieved from the CLD treatments is just one example of what can be obtained from the final package of noise controls. As mentioned above, previous lab results showed a 1-dB reduction in overall A-weighted sound power levels from the CLD plates alone
The authors would like to thank the employees at our partner preparation plant for their assistance with our field study, and NIOSH OMSHR employees: Pat McElhinney and Jeff Yonkey for their assistance with the field testing, Vincent Conteen and Andy Lawczniak for preparing the CLD plates for installation, Vincent Conteen for modifying the spring inserts, and Lynn Alcorn for help with the TUMS installations.
The findings and conclusions in this report are those of the author(s) and do not necessarily represent the views of the National Institute for Occupational Safety and Health. Mention of any company name, product, or software does not constitute endorsement by NIOSH.
This is the fourth paper published in NCEJ on the special topic of Mining Noise.
A horizontal vibrating screen used to process coal viewed from (a) feed end and (b) discharge end.
Thermocouple locations on the vibrating screen mechanism housings. (a) Left mechanism locations (b) Right mechanism locations.
1/3-Octave-band plot of A-weighted sound power levels of the unmodified Conn-Weld 8′ × 16′ horizontal vibrating screen.
Examples of small (left) and large (right) spring inserts. Note that the metal backing plate has been removed from the small spring insert.
Constrained layer damping treatments applied to the top and front faces of the mechanism housings.
Model of TUMS system (a) and picture of TUMS system installed on the vibrating screen (b).
Illustration showing placement of the H-beam cap, vibration isolators, and raft.
Illustration of Tuned Mechanism Suspension vibration isolators.
Steel frame for the second enclosure showing (a) one frame section and (b) the entire frame assembly with most panels installed on a vibrating screen.
Enclosure installed on vibrating screen.
1/3-Octave-band plot of A-weighted sound power levels of the baseline screen vs. the screen with constrained layer damping plates and spring inserts installed.
Spacers installed above and below the top portion of the vibration isolators.
A-weighted sound power for baseline vs. four iterations of the tuned mechanism suspension (TUMS).
A-weighted sound power comparison for all configurations tested.
Comparison of 330.30-L/s (700-CFM) exhaust fan configurations with baseline and enclosure only configurations.
Plan view of microphone positions and barrier-absorber curtain location surrounding screen #169.
Microphone positions 3–6 on the left side of the screen.
Example of seal around pipes through the barrier wall.
Barrier wall surrounding the screen.
1/3-Octave-band sound pressure level comparison with screen #169 shut down, with and without the barrier-absorber material installed.
Spring inserts in place and springs installed on the vibrating screen.
1/3-Octave-band sound pressure level comparison with all equipment running with barrier-absorber material installed, with and without noise controls.
A-weighted sound power levels for successful tuned mechanism suspension (TUMS) iterations. The baseline configuration included constrained layer damping on the mechanism housings and spring inserts.
| Durometer | Top Washer | Bottom Washer | A-weighted Sound Power Level (dB) |
|---|---|---|---|
| N/A (Baseline) | N/A (Baseline) | N/A (Baseline) | 97.8 |
| 80 | 1/4 in. | 1/8 in. | 97.0 |
| 80 | 1/4 in. | None | 96.4 |
| 90 | 1/8 in. | 1/8 in. | 96.8 |
| 90 | 1/8 in. | None | 96.4 |